Failure Analysis of Condenser Tube in Unit 1 of the Tenayan Steam Power Plant 2 X 110 MW
- DOI
- 10.2991/iccelst-st-19.2019.13How to use a DOI?
- Keywords
- Condenser, Erosion Corrosion, RCFA, turbidity, dent
- Abstract
This study conducted a failure analysis of the condenser tube in unit 1 of the Tenayan Steam Power Plant. It started from the inspection in the first year after the commercial off date (COD) where there is a leaky tube, so there is further suspicion. Various tests and analysis are carried out such as tube vacuum testing, Eddy current testing, condenser tube material analysis, condenser water quality analysis, effectiveness and heat transfer on a condenser to the determination of root cause failure analysis to ensure condenser performance. From the results obtained, the cause of the failure of the condenser tube in unit 1 is the thinning of the condenser tube wall. The failure mechanism is erosion corrosion caused by the use of water in condensers that contain high turbidity.
- Copyright
- © 2019, the Authors. Published by Atlantis Press.
- Open Access
- This is an open access article distributed under the CC BY-NC license (http://creativecommons.org/licenses/by-nc/4.0/).
Cite this article
TY - CONF AU - Nur Rohman Aziz AU - Ahmad Kafrawi Nasution AU - Ridwan Abdurrahman PY - 2019/12 DA - 2019/12 TI - Failure Analysis of Condenser Tube in Unit 1 of the Tenayan Steam Power Plant 2 X 110 MW BT - Proceedings of the International Conference of CELSciTech 2019 - Science and Technology track (ICCELST-ST 2019) PB - Atlantis Press SP - 65 EP - 69 SN - 2352-5401 UR - https://doi.org/10.2991/iccelst-st-19.2019.13 DO - 10.2991/iccelst-st-19.2019.13 ID - Aziz2019/12 ER -